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************************************************************
NTSB ADVISORY ************************************************************ National
Transportation Safety Board Washington, DC
20594 October 26, 2009 ************************************************************ NTSB ISSUES
UPDATE ON ITS INVESTIGATION OF FLIGHT 188 THAT OVERFLEW INTENDED
MINNEAPOLIS AIRPORT ************************************************************ In its continuing
investigation of an Airbus A320 that overflew the
Minneapolis-St Paul International/Wold- Chamberlain
Airport (MSP), the National Transportation Safety Board has
developed the following factual information:
On Wednesday, October 21, 2009, at 5:56 pm mountain daylight
time, an Airbus A320, operating as Northwest
Airlines (NWA) flight 188, became a NORDO (no radio
communications) flight at 37,000 feet. The flight was operating as a
Part 121 flight from San Diego International Airport, San
Diego, California (SAN) to MSP with 144 passengers, 2
pilots and 3 flight attendants. Both pilots were
interviewed separately by NTSB investigators
yesterday in Minnesota. The following is an overview of the
interviews: * The
first officer and the captain were interviewed for over 5 hours
combined. * The
Captain, 53 years old, was hired in 1985. His total flight time
is about 20,000 hours, about 10,000 hours of A-320
time of which about 7,000 was as pilot in command. * The
First Officer, 54 years old, was hired in 1997. His total flight
time is about 11,000 hours, and has about 5,000 hours
on the A-320. * Both
pilots said they had never had an accident, incident or
violation. * Neither
pilot reported any ongoing medical conditions. * Both
pilots stated that they were not fatigued. They were both
commuters, but they had a 19-hour layover in San Diego just
prior to the incident flight. Both said they did not fall
asleep or doze during the flight. * Both
said there was no heated argument. * Both
stated there was a distraction in the cockpit. The pilots said
there was a concentrated period of discussion where
they did not monitor the airplane or calls from ATC
even though both stated they heard conversation on
the radio. Also, neither pilot noticed messages that
were sent by company dispatchers. They were discussing
the new monthly crew flight scheduling system that was
now in place as a result of the merger. The
discussion began at cruise altitude. * Both
said they lost track of time. * Each
pilot accessed and used his personal laptop computer while
they discussed the airline crew flight scheduling
procedure. The first officer, who was more familiar with the
procedure was providing instruction to the
captain. The use of personal computers on the flight deck is
prohibited by company policy. * Neither
pilot was aware of the airplane's position until a flight
attendant called about 5 minutes before they were
scheduled to land and asked what was their estimated time of
arrival (ETA). The captain said, at that point, he
looked at his primary flight display for an ETA and
realized that they had passed MSP. They made contact with
ATC and were given vectors back to MSP. * At
cruise altitude - the pilots stated they were using cockpit speakers
to listen to radio communications, not their
headsets. * When
asked by ATC what the problem was, they replied "just
cockpit distraction" and "dealing with company issues". *
Both pilots said there are no procedures for the flight attendants
to check on the pilots during flight. The Safety Board
is interviewing the flight attendants and other company
personnel today. Air traffic control communications
have been obtained and are being analyzed. Preliminary data
from the cockpit voice recorder (CVR) revealed the
following: * The
CVR recording was 1/2 hour in length. * The
cockpit area microphone channel was not working during this
recording. However, the crew's headset microphones
recorded their conversations. * The
CVR recording began during final approach, and continued while
the aircraft was at the gate. * During
the hours immediately following the incident flight, routine
aircraft maintenance provided power to the CVR for a few
minutes on several occasions, likely recording over
several minutes of the flight. The FDR captured
the entire flight which contained several hundred aircraft
parameters including the portion of flight where there was
no radio communication from the flight crew.
Investigators are examining the recorded parameters to see if any
information regarding crew activity during the portion of flight
where radio contact was lost can be obtained. The Safety
Board's investigation continues. ### NTSB Media
Contact: Keith Holloway, (202) 314-6100 hollowk@xxxxxxxx ************************************************************ This message is
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